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Low boost at low rpm MHD stg2+ logs
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02-17-2017, 12:20 PM | #1 |
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Low boost at low rpm MHD stg2+ logs
Hi guys
I am a new member on this forum from South Africa, but I have been lurking for a while. I am hoping that someone can assist me with what exactly could be wrong with my car. It is a 2007/08 335i E92 6AT. Mods are as follows: Catless DP's Custom exhaust Cobb charge pipe AA sport FMIC BMS DCI The problem is that the car is just not performing at low rpm. After 4000rpm it feels like the boost just hits hard. The car was recently walnut blasted. The car does have wastegate rattle at low rpm and light throttle and on decel. It is almost as if the wastegate is not closing fully but I am not sure what the problem is. Here is an attached dyno graph with a local flash tune on E40 fuel. If you look at the shape of the torque curve, it is just not what it should be. This is not the file as i've seen many other N54's with the same tune with different torque curves. I also logged for the first time today, 3rd gear pulls. These logs are with MHD stage 2+ 95RON with 95RON fuel. At higher rpm I noticed the LPFP dipping into 40s and hitting as low as 39psi. I've read that anything below 50psi is not good, but I am no expert. Any help with the low boost issue will be much appreciated http://datazap.me/u/nikhyg/mhd-stg2-...og=0&data=3-21 http://datazap.me/u/nikhyg/mhd-stg2-...og=0&data=3-21 |
02-17-2017, 12:36 PM | #2 |
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Hard to tell on my phone, but your fuel trims seem high and you definitely need to upgrade your lpfp if you want to run that much ethanol. Your IATs are pretty high too, at least on the first log. Didn't look at the 2nd one
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02-17-2017, 01:00 PM | #3 |
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Wow comparing this: http://datazap.me/u/nikhyg/mhd-stg2-...&data=2-3-5-21 To my: http://datazap.me/u/aqid/mhd-stage-2...&data=2-3-5-22 Seems like we have the same slow build in boost. I posted this log yesteday in the MHD topic since I also felt it wasn't what it was supposed to be. Mine feels the same, before 3.5k RPM not a lot of power, after that it pulls hard. So far I've been thinking boost solenoids, vacuum lines or leaking DV's. I also have some WG rattle, which leads me to believe it might not have enough vacuum. I had a broken vacuum canister at the end of last year, causing the boost to drop to 0. During that time the WG rattle was horrid.
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2007 335i e92: Avant Garde M310 • MHD Stg2+ • Mr. 5 intake • VRSF DP • VRSF FMIC • Dtec v7 Angel Eyes • iJDMTOY 6k HID
2017 X6M F86: Still stock ![]() Last edited by Aqid; 02-17-2017 at 01:08 PM.. |
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02-17-2017, 01:48 PM | #4 |
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omg OP you are running outrageously lean! After looking at those STFTs, please for the love of God, reset all adaptations before you blow something up.
As mentioned, you likely have tired solenoids and/or vacuum leaks. Might as well check for boost leaks while you're at it too. Look to buy an upgraded LPFP in the meantime. |
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02-17-2017, 02:01 PM | #5 | |
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2007 335i e92: Avant Garde M310 • MHD Stg2+ • Mr. 5 intake • VRSF DP • VRSF FMIC • Dtec v7 Angel Eyes • iJDMTOY 6k HID
2017 X6M F86: Still stock ![]() |
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02-17-2017, 03:22 PM | #6 | |
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02-18-2017, 01:26 AM | #7 | |
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madmantwo Thank you for your input
Aqid Our boost issue looks the same. I am hoping that it is just a vacuum leak or solenoids and nothing to do with the wastegate bushings, flapper arms etc. Quote:
http://datazap.me/u/nikhyg/18feb-stg...og=0&data=3-21 http://datazap.me/u/nikhyg/18feb-stg...og=0&data=3-21 http://datazap.me/u/nikhyg/18feb-stg...og=0&data=3-21 http://datazap.me/u/nikhyg/18feb-stg...og=0&data=3-21 |
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02-18-2017, 01:46 AM | #8 |
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Just looked at the first log... your short term fuel trims are off the charts and you're running very lean. IATs are high too, probably should get a bigger intercooler. I would not run E40 anymore if I were you, I tried E30 back when I had stock LPFP and it just couldn't handle it. Some cars can, some just can't. I'd try a more conservative tune for now and see if you can get the fueling sorted out, then upgrade your LPFP and try gradually getting more aggressive. At this rate you'll melt something.
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02-18-2017, 02:06 AM | #9 | |
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Last edited by STREET_B335T; 02-18-2017 at 02:07 AM.. Reason: spelling errors |
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02-18-2017, 02:58 AM | #11 | |
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2007 335i e92: Avant Garde M310 • MHD Stg2+ • Mr. 5 intake • VRSF DP • VRSF FMIC • Dtec v7 Angel Eyes • iJDMTOY 6k HID
2017 X6M F86: Still stock ![]() |
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02-18-2017, 04:13 AM | #12 | |
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02-18-2017, 09:49 AM | #14 |
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madmantwo The fuel seems decent judging by timing corrections. It's Shell Vpower branded 91oct/95ron
Going to go with Boost Concepts LPFP. Hoping this solves the lean AFR issue. Thanks for the help Last edited by STREET_B335T; 02-18-2017 at 09:51 AM.. Reason: Correction |
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03-15-2017, 09:07 AM | #15 |
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UPDATE:
Fitted Boost Concepts LPFP and the LPFP psi is looking much better. Also replaced one boost solenoid for now, the old one was actually broken.. ![]() Flashed MHD E40 v5.1 and did a log. Boost seems way under target. Any help will be much appreciated http://datazap.me/u/nikhyg/mhd-e40-v...data=3-5-16-21 |
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03-15-2017, 11:31 AM | #17 |
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Thanks @FCobra94
Will do that. Only replaced one because that one was broken. But going to replace the other one and log again. Is the fuel trims and AFR okay? |
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03-15-2017, 01:28 PM | #18 | |
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Its nice for the n54 community to be so helpful. Your AFR is still not good, that why he asked you to reset adaptations. Also please check your vacuum hoses. |
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03-19-2017, 03:25 AM | #19 |
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Got another new boost solenoid and here is some updated logs:
http://datazap.me/u/nikhyg/e40-v51-l...3-5-9-15-16-21 http://datazap.me/u/nikhyg/e40-v51-l...data=3-5-15-21 |
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03-19-2017, 04:03 AM | #20 | |
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Also would not run V5.1 maps as they have desensitised knock tables AFAIK. just YouTube "desensitised knock tables vtt" and see how that ended ![]() |
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03-19-2017, 09:46 AM | #21 |
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I have the same logs as yours.
My problem is boost leak, my outlet has a hole. So please check your pipes: outlet intercooler chargepipe and their connectors good luch |
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04-17-2017, 03:05 PM | #22 |
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Hi guys
Still battling this issue. I had all the vacuum lines replaced. Logged again and it didn't make a difference. I then swopped out the diverter valves with another pair and the logs were still the same. I'm thinking it will have to be sent somewhere to do boost leak and vacuum testing. I read up a bit on the vacuum testing. Any more advice on these tests? Here are the latest logs: http://datazap.me/u/nikhyg/log-14924...=0&data=3-5-21 http://datazap.me/u/nikhyg/mhd-stg2-...=0&data=3-5-21 |
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