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BMW 3-Series (E90 E92) Forum
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MHD N55 Stage 1 Possible Boost leak?
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05-31-2024, 05:50 AM | #23 | |
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Mods are: chargepipe and next week FMIC |
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05-31-2024, 09:38 AM | #24 |
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Drives: 2015 BMW X1 35i M-sport
Join Date: Mar 2021
Location: Twin Cities MN
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Not sure about the virtual dyno numbers, but I can say that when I went from stock to stage 1 I couldn't really feel a difference. The biggest bump in performance that I could actually tell a difference was getting my catless downpipe.
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06-04-2024, 05:02 AM | #25 | ||
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Did you then do 15 and 29 as there doesn't seem to be a gasket coming from the compressor for the tube into the intercooler? I've already replaced 17 and 19 and have the VRSF chargepipe. Is it worth replacing anything else upstream of the turbo like the one for the MAF sensor 3? This is what I'm using for reference on a 03/2012 UK N55 on 124k miles https://www.realoem.com/bmw/enUS/sho...diagId=13_1357 I'm going to take it into a shop next week for shifter bushes and diff fluid change and they're going to diagnose it too. Is it worth preparing for the fact that the turbo to intercooler pipe could have a crack or even the turbo inlet? |
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06-04-2024, 09:18 AM | #26 |
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Today I changed the gaskets from the intercooler and from the turbo outlet to intercooler and now it's holding boost as it should for a PWG, so problem solved
Malteser_wfj , for the pressure sensor I used a gasket from a set, Inner diameter of 9mm and thickness of 2mm. I did 15 and 29 from that diagram and also today I changed the turbo outlet to intercooler gasket with 11618506782, I couldn't find it in the diagram and just ordered this one to try and it worked. And also, the two gaskets that go on each side of the intercoooler. If I were you, I would check first the gaskets. My 2011 has around the same miles as yours and the pipes are in very good shape. The gaskets might be done because time and also heat has destroyed them. Please keep us updated if this worked for you also, so others can see. Also, when you are datalogging, do it in 3rd gear and WOT from 2000-2500 rpm and right after you change to 4th stop the datalog. That's how we can see accurately what is going on on your car. |
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Malteser_wfj70.50 |
06-04-2024, 01:11 PM | #27 |
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Thanks for the reply minulache , I've gone ahead and ordered 3, 19, and 15 as well as the part you had listed 11.61.8.506.782 and they should be with me next week direct from BMW.
I'll try and log some more pulls this week and will be sure to do them in 3rd and go WOT sooner in the rpm range. I think it's curious how my leak appears to start only at around 4700rpm. Or that's when the STFT start shooting into the negative. Next up I'm going to replace the vacuum pipes over summer anyway - 11657588771 11657588773 11657605416 Thank you for all your help and I'm glad that it's fixed your leak!! |
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minulache64.00 |
06-05-2024, 05:18 PM | #28 | |
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Car is going in on Tuesday next week so will update on any findings https://datazap.me/u/lemansn55/log-1...og=0&data=4-20 https://datazap.me/u/lemansn55/log-1...og=0&data=4-20 My fuel pressure is dropping as the revs increase, is that normal or potentially a weak LPFP? Last edited by Malteser_wfj; 06-05-2024 at 05:24 PM.. |
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06-09-2024, 02:43 PM | #29 |
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So, I noticed that now my boost is very good after all the changes BUT my WGDC hits 100%... any idea what I should look for? I think it's clear that there is no boost leak given the boost pressure now. Maybe the pressure converter or boost solenoid?
https://datazap.me/u/minulache/0906-...og=0&data=4-17 |
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06-19-2024, 04:34 PM | #30 |
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Fixed finally. Changed the boost solenoid/pressure converter and the boost is alot better. See log.
https://datazap.me/u/minulache/1906-1?log=0&data=4-5-17 |
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wrevilo82.50 Malteser_wfj70.50 |
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