|
|
|
|
|
|
BMW Garage | BMW Meets | Register | Today's Posts | Search |
|
BMW 3-Series (E90 E92) Forum
>
MHD "take a look at my log" thread
|
|
06-30-2018, 01:42 PM | #2245 |
Private First Class
50
Rep 139
Posts |
Or the old fashion way: “please take a look at my logs” - I have two. One is mhd 2+ 91 oct. and the other is e25.
IC, DP, inlets and outlets. Have an audible whooshing leak I believe could be coming from an outlet, and some tiny leaks at the IC passenger side connect and stock diverters(at the base connection not diaphragm leak) - also front turbo rattle has gotten worse, even after having the wastegate arm shimmed to tighten things up. Trying to identify if I have a boost leak(which seems the most obvious) - or if my 65k mile front turbo is weak. Rear turbo is new from BMW warranty replacement 10k miles ago. 91 OCT 2+ https://datazap.me/u/drunkentrader/m...23-24-25-30-31 E25: https://datazap.me/u/drunkentrader/m...-31&mark=27-20 |
Appreciate
0
|
07-03-2018, 09:18 PM | #2246 |
Banned
18
Rep 115
Posts |
Maybe someone can tell me if all is well on my chart? I have zero idea how to read a chart. E93, Stage 2+ tune, xhp stage 3 tranny flash, dinan CAI, VRSF 5inch IC, VRSF DP, HKS bov VRSF Chargepipe.
https://datazap.me/u/rediahad/log-15...og=0&data=3-23 |
Appreciate
0
|
07-04-2018, 10:16 AM | #2247 | |
Private First Class
61
Rep 146
Posts |
Quote:
|
|
Appreciate
0
|
07-04-2018, 03:11 PM | #2248 |
OG
4
Rep 23
Posts |
Hello everyone, I ran a log recently and I've noticed that there are some issues in the log. There seems to be a fair amount of timing corrections in the logs and I've never seen that type of issue in my previous logs. Also I'm under boosting about 2 psi from target and maybe somehow that may be related to the timing corrections.
Recent maintenance: changed oil about 500 miles ago. Replaced all coil packs and one spark plug specifically on cylinder 2 due to misfires. Mods: vrsf downpipes and 7in intercooler, ssr intakes, synapse cp and bov, 335is/smfw clutch and flywheel, fuel-it stage 2 bucketless lpfp, mhd stage 2 e60 ots Also no codes were thrown during these logs. I'm not very good yet at diagnosing things but maybe someone could point me in the right direction? Thanks for the help! https://datazap.me/u/jonathane92/e60...-race-m4?log=0 There's 3 logs in there. I believe the 3rd to 5th gear pull I raced my friends m4 and I got pretty bad shift bog between 3rd and 4th.
__________________
N54 FBO, PURE600, MOTIV CUSTOM TUNE E30
|
Appreciate
0
|
07-08-2018, 03:53 AM | #2249 |
First Lieutenant
72
Rep 367
Posts |
Does this look like a boost leak? Car feels a little slow but WG duty is not anywhere near maxed and this is an OTS map for 91acn
https://datazap.me/u/blown95impalass...=1&data=3-5-23 edit: also just noticed I don't full hit boost target until almost 5k Last edited by Blown95ImpalaSS; 07-08-2018 at 01:32 PM.. |
Appreciate
0
|
07-09-2018, 12:40 PM | #2250 | |
Colonel
668
Rep 2,074
Posts |
Quote:
__________________
335i e92 TPC 19Ts
|
|
Appreciate
2
Blown95ImpalaSS71.50 |
07-09-2018, 01:59 PM | #2251 |
First Lieutenant
72
Rep 367
Posts |
Thanks for the reply. I'm gonna do boost control solenoids since they are original and hunt for small leaks this weekend. Given the turbos are OEM w/133k this may be all they've got
|
Appreciate
0
|
07-09-2018, 04:29 PM | #2252 |
Registered
0
Rep 1
Posts |
Boost leak or...?
Hi all! This is my first post here.
I bought this car over a month ago and also bought MHD flasher and I've been running stage 1+ for about 3 weeks. It pulled really hard at first but I began to notice it wasn't pulling as hard. At first I thought it was just me getting used to the extra horsepower, but then I got an 30ff code (and I've been getting it every time I go WOT through 3rd gear since). Never quite hit target and boost drops off like a rock. I've since downgraded the tune back to Map 0 (stock) and I am still getting the code. I'm wondering what my logs tell you guys. Turbos gone bad? Boost pressure solenoid? I've never had any wastegate rattle. I've checked the charge pipe and it is perfectly in-tact. Looking into other possible sources. Thanks you so much for looking! https://datazap.me/u/dillonl/log-153...=0&data=3-5-21 |
Appreciate
0
|
07-11-2018, 01:56 AM | #2253 |
New Member
1
Rep 27
Posts |
Someone take a look at my log and tell me what’s wrong with it please. I’m getting so serious issues.
https://datazap.me/u/blake11545/some...og=0&data=3-24 |
Appreciate
0
|
07-11-2018, 06:30 AM | #2254 |
New Member
18
Rep 27
Posts |
Hey guys,
-8.7 degrees of timing correction on cylinder 4... any idea what could cause this? https://datazap.me/u/dannybeckett/v7...data=3-8-11-24 |
Appreciate
0
|
07-11-2018, 07:35 AM | #2255 | |
New Member
18
Rep 27
Posts |
Quote:
https://datazap.me/u/dannybeckett/v8...-12-13-24&hg=1 What a difference.... |
|
Appreciate
0
|
07-11-2018, 10:44 AM | #2256 | |
Lieutenant Colonel
486
Rep 1,550
Posts |
Quote:
Are your injectors original? |
|
Appreciate
0
|
07-11-2018, 12:11 PM | #2257 | |
Major
87
Rep 1,448
Posts |
Quote:
|
|
Appreciate
0
|
07-11-2018, 02:23 PM | #2258 |
New Member
1
Rep 27
Posts |
|
Appreciate
0
|
07-11-2018, 02:24 PM | #2259 |
New Member
1
Rep 27
Posts |
|
Appreciate
0
|
07-11-2018, 02:38 PM | #2260 | |
Lieutenant Colonel
1049
Rep 1,667
Posts |
Quote:
|
|
Appreciate
0
|
07-12-2018, 02:47 AM | #2261 |
Registered
0
Rep 3
Posts |
Hey everyone. New member. Was recommended this forum by the 335i mods page on FB.
Anywho. I'm getting bad timing corrections after flat foot shifting, and my hpfp is dipping under 1000psi. Hopefully I can get some insight on if my log looks okay. I know very very basic stuff about this. Main mods are: VRSF 7in HD intercooler, catless downpipes, relocated inlets, PSP outlets, MHD E50 v8 beta, stage 2 lpfp, Ngk 1 step colder plugs and the wotbox. Thank you in advance! https://datazap.me/u/kbro88/log-1530...og=0&data=3-21 |
Appreciate
0
|
07-12-2018, 03:19 AM | #2262 |
Lieutenant Colonel
486
Rep 1,550
Posts |
|
Appreciate
0
|
07-12-2018, 09:46 AM | #2263 | |
Private First Class
61
Rep 146
Posts |
Quote:
|
|
Appreciate
0
|
07-12-2018, 01:03 PM | #2264 |
New Member
1
Rep 27
Posts |
|
Appreciate
0
|
07-12-2018, 01:24 PM | #2265 | ||
Registered
0
Rep 3
Posts |
Quote:
I have no symptoms of my hpfp going bad. the pressure dips that low when I flat foot shift only. it will not do it when I shift normally. my afr doesn't lean out when the pressure gets low either. what is weird is that is stays at a constant 10.28 for a bit before reading other numbers. I'll get another log later today doing a pull without flat foot shifting |
||
Appreciate
0
|
07-12-2018, 04:25 PM | #2266 |
Registered
0
Rep 3
Posts |
https://datazap.me/u/kbro88/good-fue...&data=2-22
https://datazap.me/u/kbro88/fuel-drop couple more logs. should I pick up a new hpfp? the fuel drop doesn't happen every time |
Appreciate
0
|
Bookmarks |
|
|