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BMW 3-Series (E90 E92) Forum
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Fried DME :(
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08-22-2019, 07:12 AM | #23 | |
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On the basis of what you describe so far, there is no reason whatsoever to be talking about getting your DME replaced. 2A17 is DTML code 30FF is underboost, a million possible causes. Is that a stored code or one that is currently present (i.e. you have a check engine light)? |
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08-29-2019, 05:00 PM | #24 | |
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1) My COBB programmer 2) BMW Carly app with OBD II connector 3) 30FF is I believe I am getting this only under high boost 17 PSI + , I have bad waste gate rattle right now so I know its not sealing up good I was just stumped by the 2A17 thanks |
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08-29-2019, 10:15 PM | #25 | |
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EDIT: just realized that I've confused you with the original poster. Your sig says 2011 328i, is that not correct? |
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08-29-2019, 11:31 PM | #26 |
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good catch , but no I do have a 328I and a E60 M5 and a 335I , I update sig. the car I am talking about on this post is my 2007 335I
Last edited by chadjones99; 09-14-2019 at 04:33 AM.. |
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08-29-2019, 11:33 PM | #27 |
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I thought a 3OFF code is loss of boost , many things can cause this but it only happens at high boost . And I thought with a wastegate that was not sealing right it could cause this...
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08-30-2019, 06:07 AM | #28 |
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No, very unlikely for wastegate rattle to cause this - it's just an unpleasant noise. There is some other reason for your 30FF - put your head in there and listen for a leak. Decaying vac lines are a common cause, loose connections from turbo to intercooler, intercooler to charge pipe, leaking diverter valves.
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09-14-2019, 04:35 AM | #29 |
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MHD app
So I changed from a COBB to the MHD app and was able to tune out the wastegate rattle for now. and I was told I would get turbo lag by doing so but got to say I cant tell.
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