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BMW 3-Series (E90 E92) Forum
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MHD "take a look at my log" thread
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09-05-2024, 11:58 AM | #6030 | |
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Hi, I have thé same problem with V10 stage 2 using MHD+ and linear throttle. No problem with v9.... V10 has definitly some serious problem ! Time for an update version!! |
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09-06-2024, 12:25 AM | #6031 |
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I posted some of my logs a while back and still have some questions about timing corrections and fuel trims. I'm seeing timing corrections across all cylinders.
https://datazap.me/u/lowrydr310/log-...4&zoom=127-250 There's a big discrepancy between bank 1 and bank 2 fuel trims, both short term and long term. Long and short trims for bank 1 are much more negative than those for bank 2. All maintenance is good (coils/plugs, good quality fuel, new LPFP and pressure sensor) the only not so good thing are the injectors. Bank 1 has three original index 1s with 160K miles. Bank 2 has two used index 12s from a wrecked car that was running well, and one Index 9. So either those Index 1s in Bank 1 are dumping too much fuel, or the bank 2 injectors aren't delivering enough fuel. How can I tell the difference? Would injector issues cause timing corrections? Also, after looking at some of the other logs posted on this thread I realized I should really get a new intercooler. I have the stock intercooler and I'm seeing 25 degree increases in some cases just over a second gear pull. |
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09-06-2024, 01:15 AM | #6032 |
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Drives: 07 bmw 335i e90
Join Date: Apr 2022
Location: Guam
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I'm still learning to read datalog. I'm running 07 bmw 335i with jb4, mhd, xhp flasher, pedalcommander stage 2lphp, index 12 injectors. 2 cone intake. PR inductive coil. Catless downpipe with muffler delete & viva stage 2 turbo with FMIC & 50mm tial blow off valveUsing 87oct. Still bogs when take off it bogs then it start pulling when turbo kicks in.
Can you tell me how does my data log |
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09-07-2024, 06:26 AM | #6033 | |
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Here’s another user reporting from 2 years ago. https://www.e90post.com/forums/showthread.php?t=1972983 |
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09-08-2024, 04:14 AM | #6034 | |||
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Today, I removed the current MHD v3.20 (Long Write back to stock) and reinstalled v2.41. First impressions are the post mid-throttle surge is gone and the car works like it should. Revs no longer fling themselves up another 500rpm after I clutch in during gear changes. That horrible lurch and driveline shock no longer happens when I suddenly lift off mid-throttle. I’ll report back if the v3.2 symptoms reappear. Else, this is the solution for me. Last edited by LastGray; 09-08-2024 at 04:21 AM.. |
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09-08-2024, 12:09 PM | #6035 |
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Ok thats a good news even if MHD multimap is important for me as i Can run ethanol mix dayli but keep possibility to Switch to gaz map if ethanol should not be able during a roadtrip for example.
If it works fine you could make a Feedback @jake and wedge and hope for a MHD version update. Let us know if everything is still ok After few hundred miles with v2.41. |
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09-10-2024, 01:20 PM | #6036 | |
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09-12-2024, 06:37 PM | #6037 | |
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09-15-2024, 07:25 AM | #6038 |
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Update on v2.41 (Android) and 200miles of driving.
I have been trying hard to emulate it and while it is not 100% gone, it feels more like a torque lump rather than v3.x’s outright driveline shock as if someone hit the pedal immediately after you lifted quickly at >40% throttle. Mind you, I’ve also set my 1M throttle lag setting to 40%. While I love the throttle response, I’ll experiment with 30% to see if it diminishes the lift-off surge further into the negligible. |
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09-18-2024, 12:18 AM | #6039 |
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Would appreciate some help diagnosing this misfire
https://datazap.me/u/tox/n54-misfire...20&zoom=79-145 I first started getting misfires on cyl1 (29CD) so I just swapped the coil pack to cyl2, now it looks like I'm getting a misfire on cylinder 4 instead (29D0). I have brand new spark plugs, running MHD stage 1 91 (with 93 in the tank), catless dp, DCI. Coils are original so I was planning on replacing them anyways, but didn't want to cover up a potentially more serious issue (or ruin a new set) if there's something else going on. The rail pressure drop and spike in AFR has me wondering if its a HPFP or injector issue..
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09-19-2024, 08:42 PM | #6040 |
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Can someone look at these logs? Trying to help a friend diagnose an issue with losing boost pressure toward the end of a pull. Only codes he gets are O2 codes. Could it be just that simple, O2 sensors? I'm concerned with his wgdc looking too high for too long, and also dropping some rail pressure psi when it starts to lose boost.
https://datazap.me/u/t0ymach1n3/log-...og=0&data=3-21 https://datazap.me/u/t0ymach1n3/log-...0&data=3-21-29 |
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09-20-2024, 02:35 AM | #6041 | |
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Too much time to reach boost target make DME ask for 100% WGDC too long then wgdc stay high to keep only 14psi @ low rpm. Around 3500rpm HPFP pressure fall and STFT reach +20%, maybe normal because of low boost so no need for lot of fuel but could be another problem too. I will start by looking at boost leak by making a smoke test. |
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09-20-2024, 02:48 AM | #6042 | |
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I don't think that you have a leaky injector because AFR reach 234 value on both bank after pedale release. |
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09-20-2024, 02:33 PM | #6043 | |
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09-23-2024, 06:36 PM | #6045 |
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Can someone check this log out. I am getting a detonation sound or rattle in the engine around 40 percent load and around 2000-2500 rpm. The sound is a direct correlation to engine timing corrections on cylinder 1 and 2. Sound goes away once the corrections go back to zero. It does not make the sound at a stand still but only when driving and loading the engine. New plugs, new coils, and index 12 injectors.
I tried different MHD tunes, but same corrections and sound. Going to go to a custom tune, but wanted you guys to let me know if you see anything sticking out. https://datazap.me/u/quadboy47/stage...ata=3-14-16-18 |
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09-25-2024, 07:17 PM | #6046 |
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[QUOTE=Quadboy47;31493064]Can someone check this log out. I am getting a detonation sound or rattle in the engine around 40 percent load and around 2000-2500 rpm. The sound is a direct correlation to engine timing corrections on cylinder 1 and 2. Sound goes away once the corrections go back to zero. It does not make the sound at a stand still but only when driving and loading the engine. New plugs, new coils, and index 12 injectors.
I tried different MHD tunes, but same corrections and sound. Going to go to a custom tune, but wanted you guys to let me know if you see anything sticking out. https://datazap.me/u/quadboy47/stage...ata=3-14-16-18[/QUOTE Has the spark plugs in 1 and 2 looked at?
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09-26-2024, 11:49 AM | #6048 |
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initial concave/step boost target issue
hi fellows,
I have an 09 e90 n54 335. I just start learning self-tune for my car. i have a question about the boost target. i attached 3 logs of my self-tune logs, i can see the initial boost target has a deep concave/step. i tried to set high load request all cross the rpm with modified BLM/LLF as below attached screenshot, but unfortunately it didn't help. i checked WedgePerformance tune's log, they all have very smooth/sharp boost target at the beginning. May i know the reason for this? thanks in advance! self-tune logs: https://datazap.me/u/dragonfly1112/s...og=2&data=3-24 https://datazap.me/u/dragonfly1112/s...og=0&data=3-24 https://datazap.me/u/dragonfly1112/s...og=1&data=3-24 Last edited by Yang Liu; 09-26-2024 at 11:56 AM.. |
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09-26-2024, 12:33 PM | #6049 |
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color of the plugs say a lot, running lean or rich. If 1 and 2 are running lean at part load, while 3 runs rich so bank 1 "averages" out ok, that is a possibility. Lean will cause corrections.
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