|
|
|
|
|
|
BMW Garage | BMW Meets | Register | Today's Posts | Search |
|
BMW 3-Series (E90 E92) Forum
>
N55 boost loss
|
|
03-26-2022, 06:13 PM | #1 |
New Member
2
Rep 28
Posts |
N55 boost loss
I have a 2011 335i X-Drive and am losing some boost. I just tuned my car to stage 1 with mhd and noticed it when I was monitoring the tune. I'm new to the bmw scene and figured the forums would be the best place to try and find a fix. The cars completely stock besides the charge pipe and I checked if that's leaking but it's not. Im about to hit 80k and I know the water pump has issues around then but I have no engine codes currently. Any info helps! Thanks!
https://datazap.me/u/robsonap/stage-...&data=3-12 (I don't think I logged this test correctly, but I'm going to do another log tonight, I heard you're supposed to do a pull from 3rd at 2 rpm, but didn't know that at the time I logged this) |
03-30-2022, 09:10 PM | #2 | |
Enlisted Member
0
Rep 34
Posts |
Quote:
|
|
Appreciate
0
|
04-03-2022, 05:38 PM | #3 |
Private First Class
33
Rep 129
Posts |
>> I checked if that's leaking but it's not
Did you pressurize the system with a proper boost leak tester? The actual vs target are pretty off.... gotta be a leak somewhere. Also: - IATs increase pretty quickly. I definitely consider an intercooler upgrade. - Seeing lot of corrections on random cylinders, and especially 5th gear. Strongly recommend you do plugs and (stock coils) if they've not been done. |
Appreciate
0
|
04-04-2022, 11:46 AM | #4 |
Major General
3095
Rep 6,495
Posts |
Did you smoke test it or just visually looking for a leak? Leaks can surface when boost is applied.
__________________
|
Appreciate
0
|
04-05-2022, 05:27 PM | #5 |
New Member
2
Rep 28
Posts |
I didn't get to smoke test it but I could see via mhd I wasn't hitting my target boost, after doing some research I found it could be the boost solenoid, I had all of the symptoms. I ordered one today and it should be here by next Monday so I'll update you guys then
|
Appreciate
0
|
04-05-2022, 06:41 PM | #6 | |
New Member
2
Rep 28
Posts |
Quote:
|
|
Appreciate
0
|
04-06-2022, 09:59 AM | #7 |
Private First Class
33
Rep 129
Posts |
Not sure why parts are being thrown at the problem... get a *proper* boost leak test and then go from there. Guessing there's a leak at the charge pipe coupler...
|
Appreciate
0
|
04-06-2022, 01:12 PM | #8 |
New Member
2
Rep 28
Posts |
I took the car to the dealership to use my warranty to see if they could find the leak and they said the car held pressure fine with no leaks, they did the smoke test. I don't just have everything sitting around to do my own smoke test. Also according to the forum I was reading the boost solenoid seems to be a common problem that most people don't even notice until they're trying to make bigger power, some even starting to fail under 50k miles. Plus it's a relatively cheap part.
|
Appreciate
0
|
04-18-2022, 02:22 PM | #10 |
New Member
2
Rep 28
Posts |
I installed the boost solenoid and still had the leak, so I figured I'd give your advice a shot and reinstalled the CP. The leak was still there. After doing more research I tried replacing the CP o-ring, still nothing. I found a diagram of the intake system and really don't see where the leak could be coming from, I'm still getting no codes and holding pressure when tested. So now I'm thinking about replacing the vacuum lines and getting a vrsf Fmic to replace all old plastic. From what I understand it could also be the diverter valve or worst case scenario crack in the intake manifold. If you have any more ideas I'd love to hear, Thanks.
|
Appreciate
0
|
04-18-2022, 03:04 PM | #11 |
Major
529
Rep 1,026
Posts
Drives: 2015 BMW X1 35i M-sport
Join Date: Mar 2021
Location: Twin Cities MN
|
Do you know what pressure they're leak testing at? Your STFT gets very negative (pulling fuel out to keep AFR on target) as your rpm's rise, which could be explained by a boost leak. For MHD OTS tunes, the actual boost generally falls pretty short of target boost, if it wasn't for your really negative STFT, I'd almost think it looks normal for stage 1 OTS tune.
|
Appreciate
0
|
04-18-2022, 03:06 PM | #12 |
Major
529
Rep 1,026
Posts
Drives: 2015 BMW X1 35i M-sport
Join Date: Mar 2021
Location: Twin Cities MN
|
A bad diverter valve could explain low boost, but it doesn't explain your negative STFT, as your're not actually leaking measured air out of the system with a bad diverter valve.
|
Appreciate
0
|
04-18-2022, 03:07 PM | #13 |
Major
529
Rep 1,026
Posts
Drives: 2015 BMW X1 35i M-sport
Join Date: Mar 2021
Location: Twin Cities MN
|
Same with your boost solenoid and wastegate vacuum system: an issue there can create low boost, but shouldn't mess with your STFT.
|
Appreciate
0
|
04-18-2022, 03:10 PM | #14 |
Major
529
Rep 1,026
Posts
Drives: 2015 BMW X1 35i M-sport
Join Date: Mar 2021
Location: Twin Cities MN
|
Are you running the stock intake? If you're running an after market pipe in the location where your MAF is, it would through off your MAF reading, and could potentially explain your negative STFT.
|
Appreciate
0
|
04-18-2022, 03:32 PM | #15 |
New Member
2
Rep 28
Posts |
I still have the stock air intake only thing I've put in was the CP. Do you think I should clean or replace the MAF? What else could cause stft?
|
Appreciate
0
|
04-18-2022, 03:50 PM | #16 | |
Major
529
Rep 1,026
Posts
Drives: 2015 BMW X1 35i M-sport
Join Date: Mar 2021
Location: Twin Cities MN
|
Quote:
It sucks to throw parts at something, I'd probably start with getting MAF cleaner and cleaning your MAF to see if that helps. And maybe see if you can find any air leaks the shop may be missing??? Have you checked the intercooler-side connection of your charge pipe with the hose clamp connection? If that's over-tightened, you can collapse the stock pipe underneath, creating a leak. You'd like to think the shop would have caught that, but who knows??? |
|
Appreciate
0
|
04-18-2022, 06:50 PM | #17 | ||
New Member
2
Rep 28
Posts |
Quote:
|
||
Appreciate
0
|
04-18-2022, 06:50 PM | #18 | |
New Member
0
Rep 5
Posts |
Quote:
HELP!! hey everyone! I have a 2008 bmw 335xi I was driving one day and all of the sudden my audio completely stopped working. I have checked the fiber optics and they all work up to the front of the car. I have disconnected the battery and let the car reset and checked all the fuses. still no sound and I have zero clue what it could be. I have no sound even with the seatbelts off and if I leave my key in the car. I also charged the battery and it read full because I read the car could have gone into power conservative mode. any info would be greatly appreciated |
|
Appreciate
0
|
04-19-2022, 07:20 PM | #19 |
Private First Class
33
Rep 129
Posts |
Two things:
- Go back to stock, eg stock CP, stock tune. Still have a problem? - Get a *proper boost leak tester* and pressurize the system and look for leaks with soapy water. The smoke test is worthless (too low pressure) IMHO. Report back, and stop throwing parts at the problem fer chrissakes. |
Appreciate
0
|
04-20-2022, 03:34 PM | #20 | |
New Member
2
Rep 28
Posts |
Quote:
|
|
Appreciate
0
|
04-20-2022, 08:02 PM | #21 | |
Enlisted Member
3
Rep 43
Posts
Drives: 2013 E92 335xi MSport
Join Date: Aug 2021
Location: New Jersey
|
Quote:
That being said, you have consistent timing corrections on all your cyls throughout your pull. Cyl 6 with the most. 1-2 or 3 deg is fine, but your car could be pulling power for knock prevention. Would highly recommend plugs and coils as your first step regardless. Check vacuum lines and PCV for leaks and make sure that chargepipe to fmic connection is cranked down good. I would lose 1-2 psi and hear a high pitched whistle when those clamps weren't tight enough. Also, did you do your pull with traction off? Doubt it would cause this but just curious. Also confirm you're running 93 octane? Just want to rule out the easy stuff and not insult your intelligence
__________________
2013 E92 335xi MSport
DOCVU+JB4|xHP Stage 3|VRSF DP|VRSF FMIC|AFe Stg2 CAI|Remus Race Exhaust|ER CP|GFB DV+| |
|
Appreciate
0
|
04-21-2022, 03:20 PM | #22 | ||
New Member
2
Rep 28
Posts |
Quote:
Is the diagram I have of the vacuum lines correct? I know the n54 has a lot of vacuum lines so this diagram seems a little bare compared to those. As for the pcv is there another way to test that other then the match test? And when pcv goes out, would I just replace the cover seal or the whole gasket? When I do the datalog I have my dtc off completely and I'm running on 93. I've heard the log is supposed to be a 3rd pull only, no other gears. If I'm doing this wrong, please let me know! Thanks again for the reply! |
||
Appreciate
0
|
Bookmarks |
|
|